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    Hanna Ovr
    8月02日

    Pest Control Software

    2
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    Rafael Marín
    -3 j

    Error moving joints simultaneously in Mobile app

    5
    0
    Tomi Ade
    -6 j

    Trouble Uploading to Nyboard - stk500_recv(): programmer is not responding

    3
    0
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    Guillaume Poncin
    6月12日

    Stuck in a reset loop...

    在 Clinic

    On a new Nybble (1_1 board) that has been working great so far, I made some small changes to the code, and somehow got it to crash in a loop - it resets ever second or so with a loud beep... And as a result, I am not able to upload new code...


    I tried various combinations of unplugging / plugging the USB cable / pressing the reset button / uploading. Nothing seems to fix it...


    Any suggestion?


    Error from Arduino tool on Mac:


    Sketch uses 592 bytes (1%) of program storage space. Maximum is 32256 bytes.

    Global variables use 9 bytes (0%) of dynamic memory, leaving 2039 bytes for local variables. Maximum is 2048 bytes.

    avrdude: stk500_getsync() attempt 1 of 10: not in sync: resp=0x0a

    avrdude: stk500_getsync() attempt 2 of 10: not in sync: resp=0x2a

    avrdude: stk500_getsync() attempt 3 of 10: not in sync: resp=0x20

    avrdude: stk500_getsync() attempt 4 of 10: not in sync: resp=0x53

    avrdude: stk500_getsync() attempt 5 of 10: not in sync: resp=0x74

    avrdude: stk500_getsync() attempt 6 of 10: not in sync: resp=0x61

    avrdude: stk500_getsync() attempt 7 of 10: not in sync: resp=0x72

    avrdude: stk500_getsync() attempt 8 of 10: not in sync: resp=0x74

    avrdude: stk500_getsync() attempt 9 of 10: not in sync: resp=0x20

    avrdude: stk500_getsync() attempt 10 of 10: not in sync: resp=0x2a

    An error occurred while uploading the sketch



    And this is what the serial monitor shows below.


    (...)

    0

    Finished!


    1024 0 103 139

    k

    ⸮

    * Start *

    Nybble

    Initialize I2C

    Connect MPU6050

    Test connection

    MPU successful

    Initialize DMP

    1226 111 3 47

    Enable DMP

    Enable interrupt

    DMP ready!


    * Assigning 1 skill addresses...

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    0

    Finished!


    1024 0 103 139

    k

    ⸮

    * Start *


    1 則留言
    0
    1 則留言
    R
    Rongzhong Li
    6月12日

    Hi,

    It seems that you modified the skill information in the InstinctNybble.h, but forgot to match the pointer array or the skill name array. You may also forget to upload the first round of code to update the memory data if the skill file is correct.


    The avrdude: stk500_getsync() attempt 1 of 10: not in sync: resp=0x0a message indicates another error that's irrelevant to the code itself. It means the connection between your computer and the robot through USB is not correct.


    You may zip your code folder and send it to support@petoi.com and I can help to debug.


    按讚
    1 則留言
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